Well, I think we lucked out on the weather again - it's been horrible here today - but at least I haven't had a lot to do outside! though I still have to take the sunroof shade out and recover that..
Thanks to Miles for not only cooking food for us, but also supplying most of it! I hope the Duchess is sleeping soundly at night now (and letting you sleep soundly too!)
Also thanks to Smiler for looking at my tracking and getting that sorted out... I needed to tweak the steering box - wheel bar a bit to re-centre the steering wheel, as when I actually got to take it for a proper spin, it was a bit out again - but managed to get that done before the MOT... at least knowing the steering box - wheel is centered, I was able to do that bit by eye. You managed to do the hard bit, getting the toe all sorted with the tracking bars which is the bit I was only able to guess when I replaced the bar a year or two ago. Sorry it was such a pain to do!
My biggest thanks though have to go to Sloth... You're a true gentleman, mate, and total nutcase... After everyone else had buggered off to peace and normality at home, he stayed back (even after his fun and games with EAS) to give me a hand to re-fit my head lining card that we had covered that morning, and then stupidly to give me a hand to swap my ABS modulator, which I had been planning to do the year before, though had since pulled apart, cleaned, and assembled with new O-rings... and ideally wanted to get done before the MOT on Monday morning, so it was checked off my list and hopefully have decent braking for good.
That task started off well, after a bit of deliberating as to the best way to get the bloody thing out, around the coolant tank, myraid of brake pipes, and all the LPG cabling that runs past the modulator block.
We were doing pretty well until we got to the brake bleeding part - which although it went pretty smoothly just took ages, since the whole modulator was previously empty or fluid and full of air! we got it all done by midnight and took it out for a test drive to see how it felt... got out on the road and 'BEEP BEEP BEEP..... ABS FAULT... TRACTION FAILURE' Shit
Nanocom reported no connection on the RHF inlet solenoid - which was very quickly followed by the air turning blue on my part, and the dread of having to pull the whole modulator block again and swap it back, because the one I'd spent so much time reconditioning was obviously faulty....
A multimeter confirmed that there was no connection, on either the inlet or outlet solenoids (according to RAVE pinout) which resulted in another round of cursing. Before deciding to get violent and rip it all apart again I managed to slide my phone down the side of the modulator and get a picture of the electrical connector... to find this:
Which was kind of bittersweet to find... good in the feeling that we hopefully didn't need to pull it all out again as it wasn't likely to be a problem in the block - but bad in the fact that if we didn't drain it, remove it, etc to straighten the pins out of the vehicle, then we were faced with a stupidly tight squeeze to get in and work, and lack of being able to see a bloody thing. And if we snapped a pin, then we would STILL have to take it all back out again.
We decided to do a trip back to my place to grab the USB endoscope camera, and some smaller tools to be able to get in there and hopefully straighten the pins.. Followed by a stop at the 24hr McDonalds on the way back, as we hadn't eaten since Morat's meaty morsels in the afternoon.
Back to the workshop by about 3am, and surgery began. With Sloth draped across the top of the engine to hold the camera and tools, and me cursing at being scratched by what seemed like everything down the side of the engine, trying to get a hand in there we started, and luckily managed to get both pins straightened out somewhat... after gingerly connecting the plug part way to see if it would go on without bending the pins again, removing it and checking everything with the camera, we figured it was all good, so fitted the connector for good, crossed our fingers and turned the key to see if the fault was gone... other than the standard beeps, and messages the dash was clear, and Nanocom reported all the faults clear, and all the solenoids as working... Hooray!
A quick whip around to pack up all the tools, some of the rubbish etc, we were gone...
My view as I was leaving...
I got back about 4:30am, went straight to bed and was then up at 9am to empty all the crap out of the RR and take it for the MOT...
Luckily, it passed with flying colours... 1 advisory for O/S/R hub seal leaking a bit... which I will get under an check - but we also swapped the tyres whilst they were off and we were bleeding the brakes, and the RHF (which went to RHR) had a bit of a brake fluid mark down it - which looks very similar to an oil stain on the tyre from the hub seal... so whilst I'll investigate, I wonder if that's what they've seen and figured it was the hub seal and not some residual fluid from where we had drips whilst removing the old modulator. Even if it is a hub seal, the rears are easy to change.
So again, thanks to all who came along - and an extra, massive thanks to Sloth for staying behind and helping me out - I literally couldn't have done it without you, and you kept me sane when i was about ready to throw things!! I owe you 2 now... one for this, and one for the all nighter on the engine swap!
The good news.... the brakes feel amazing.. .I just hope they stay like that, and not lose their feel like they used to with the old modulator - because if they do the same, then I'm back at square one!
Marty
'06 4.2 Supercharged Black/Cream "Jess" -- Bought April 2021 (NZ)
'01 4.6 Vogue Black/Lightstone "Snog" -- Bought Jan 2012
'99 4.6 HSE Cobar Blue/Lightstone -- Sold March 2009
'95 4.6 HSE Epsom Green/Tan -- Traded June 2008